久久精品精选,精品九九视频,www久久只有这里有精品,亚洲熟女乱色综合一区
    分享

    [FAQ] Proper RC Snubber Design for Motor Drivers

     LC書房齋 2024-04-07 發(fā)布于浙江
    Other Parts Discussed in Thread: DRV8343-Q1, CSD18540Q5B

    Proper RC Snubber Design

    When switching high currents through external power MOSFETs to commutate a BLDC motor, ringing can occur, leading to concerns in electromagnetic interference (EMI), circuit jitter, excessive power dissipation, and overstressing components. This is often due to parasitic inductances and capacitances in the Printed Circuit Board (PCB), specifically in the high-current-carrying phase nets between the high-side and low-side MOSFETs. Inductors and capacitors form an inductor-capacitor (L-C) tank circuit, resulting in resonance during switching events.

    Figure 1 – Ringing at motor phase output due to L-C tank resonance

    In order to mitigate the ringing at the phase output, a simple resistor-capacitor (R-C) snubber circuit can be used to “snub”, or dampen the oscillations. By removing the oscillations, this will reduce potential EMI and increase the longevity of the MOSFETs by reducing voltage overstress. The R-C snubber is placed in parallel as close as possible to each MOSFET’s drain and source connections.

    Figure 2 – RC Snubber

    To calculate the resistor (Rsnub) and capacitor (Csnub) values of the R-C snubber circuit, we will use a 7-step procedure that shifts the resonant frequency of the MOSFET ringing to calculate the circuit’s parasitic capacitance (C0) and inductance (L). Once those are known, they will be used to derive the values of the R-C snubber. The example shown uses the RC snubber next to the CSD18540Q5B MOSFETs (Qgd = 6.8nC) of the DRV8343-Q1 EVM.

    Figure 3 – Measure fo of VDS ringing without RC snubber

    Figure 4 – Measure f1 of VDS ringing with C0 = 100pF

    Figure 5 – MOSFET ringing is dampened using calculated RC snubber values

    Figure 5 shows the spike reduction and damping effect of the calculated R-C snubber values. You can adjust the ringing higher or lower by varying the Csnub value. Larger values for Csnub reduce the voltage-spike amplitude further, but increase power loss in Rsnub.

    Alternatively, you can decrease the power dissipation in Rsnub by lowering Csnub, but ringing will increase. You must weigh the trade-off between acceptable voltage-ring amplitude and Rsnub losses.

    If a positive or negative voltage transient appears at the VDS switching event after snubbing out the ringing effects, you can lower the source current into the MOSFET gate or the sink current from the MOSFET gate. This will increase the rise and fall time of the MOSFET switching and reduce the maximum transient spike. It is important to monitor negative voltage transients when switching a MOSFET off to not exceed any maximum negative transient specifications of the gate driver device.

      本站是提供個人知識管理的網(wǎng)絡(luò)存儲空間,所有內(nèi)容均由用戶發(fā)布,不代表本站觀點。請注意甄別內(nèi)容中的聯(lián)系方式、誘導(dǎo)購買等信息,謹防詐騙。如發(fā)現(xiàn)有害或侵權(quán)內(nèi)容,請點擊一鍵舉報。
      轉(zhuǎn)藏 分享 獻花(0

      0條評論

      發(fā)表

      請遵守用戶 評論公約

      類似文章 更多

      主站蜘蛛池模板: 天天做天天爱天天综合网2021| 一級特黃色毛片免費看| 欧洲免费一区二区三区视频| 两个人看的视频WWW在线高清| 东京热TOKYO综合久久精品| 国产偷窥熟女高潮精品视频| 少妇人妻无码专区视频| 久久99国产精品尤物| 久久月本道色综合久久| 99RE6在线观看国产精品| 人妻丝袜中文无码AV影音先锋专区| 18禁超污无遮挡无码网址极速| 日韩中文字幕高清有码| 午夜宅男在线永久免费观看网| 爽爽影院免费观看| 亚洲www永久成人网站| 精品 日韩 国产 欧美 视频| 欧美黑人又大又粗XXXXX| 亚洲色欲色欱WWW在线| 国产精品普通话国语对白露脸 | 国内精品久久久久影院网站| 少妇又爽又刺激视频| 美女裸体18禁免费网站| 国产精品国产三级国快看| 秋霞电影院午夜无码免费视频| 国产又爽又黄无码无遮挡在线观看| 国产精品一码二码三码| 国产成AV人片在线观看天堂无码| 欧美性受XXXX黑人XYX性爽| 国产成人高清精品亚洲| 精品一区二区三区免费播放| 一本一道VS无码中文字幕| 成人做受视频试看60秒| 亚洲国产午夜精品理论片妓女| 成人欧美一区二区三区的电影| 人妻系列中文字幕精品| 日本边添边摸边做边爱的视频| 免费人成在线观看成人片| 国产日韩一区二区四季| 色窝窝无码一区二区三区| 波多野结衣久久一区二区|